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#1
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Hi all, just wondering why my scoob has low boost. 7psi, its running about 290bhp, its a 93 wrx.. why I ask is my other scoob was running 14psi.. ive got the same ecu and everything else, any ideas
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#2
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Checked all the boost pipes?
What's the reading at Idle? Has someone changed bottom pipe on the 3 port?
__________________
2001 Bugeye - Project Black/Red, 1997 JDM Type R, 1995 V1 WRX, Defender Tithonus MOD Styleeee! |
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#3
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no boost leeks, -20 on idle. no bottom pipe not changed. - 20 is what other scoob idles at too
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#4
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Any faults stored?
__________________
2001 Bugeye - Project Black/Red, 1997 JDM Type R, 1995 V1 WRX, Defender Tithonus MOD Styleeee! |
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#5
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no. ive even swapped the BCS.s over
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#6
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Blow down the pipe the runs to the actuator, if you can blow, the diaphragm inside is gone. Swapped one over for a guy on Surrey at the weekend just gone.
__________________
2001 Bugeye - Project Black/Red, 1997 JDM Type R, 1995 V1 WRX, Defender Tithonus MOD Styleeee! |
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#7
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will try that
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#8
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done the above test. actuator working fine
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#9
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Boost gauge plumbed into the wrong pipe.
Your reading actuator cracking pressure rather then manifold pressure. |
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#10
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Boost gauge plumbed into manifold
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#11
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Well you won't be getting 290BHP from 7psi.
That's more like a figure generated by 16psi (and even that's if everything is top notch w.r.t MAF, Plug's, Coilpacks, Fuel Pump, Turbo and compression). |
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#12
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when it went to surry rolling road last year the print out says 290. but it had good boost then. its just dropped for some reason
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#13
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Probably a knackered MAF then if the CEL hasn't come on.
Sometimes cleaning the MAF with carb cleaner will bring it back temporarily. |
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#14
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ok will try that, thanks
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#15
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The early MY92-96 have a tendency to drop the boost target down to protect the car when it spots a MAF fuelling issue. It doesn't normally throw up a CEL either.
If you can boz one from someone else it could be worth a pint........ |
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#16
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I have a maf from my classic, had it removed when daughterboard was fitted, was working fine before that.
if you need to test |
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#17
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I had this scott if you remember we fitted dawes device to compensate
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